David, at 200 steps per revelolution the motor will run rough. Once you get it running change the dip switches on the driver to 1/8th step or 1600 pulses/rev. It will run much smoother.
Mark
David, at 200 steps per revelolution the motor will run rough. Once you get it running change the dip switches on the driver to 1/8th step or 1600 pulses/rev. It will run much smoother.
Mark
Last edited by mark_s; - 29th September 2020 at 00:05.
Mark thanks for the info. I'm new to working with stepper motors and their controllers. Seems a little easier to use a controller than to do all the programming to pulse all 4 inputs on the motor manually.
It looks like the NEMA rating just has to do with the size of the front or something here is the NEMA 23 one I got. It looks like this is rated 2.8 amps so would you mind I should set my controller dip switches to reflect 2.8 amps right?
Thanks
David
Normally I would design and build everything necessary to perform the tasks I need to with a PIC. In this case though to speed up development of my project I decided to use the stepper motor controller and relay module I am using to speed things up. The PIC is still doing all the work. I am working on a conveyer belt system that will move parts under a sprayer to get coated with a substance. I am controlling a solenoid to turn air on and off and a second solenoid to control dispensing the liquid, in this case for testing it is water. One thing I noticed since the nozzle is gravity fed and upside down as seen in my video, the gravity feed will produce a stream of water when the air is not engaged basically a constant drip so controlling the liquid flow (on and off) eliminates the drip. I did find no drip nozzles where I would only need to control the air flow but at $400 a pop that was not going to happen. The ones I am using are $20. My video is a mock up model for testing. I plan on adding a small conveyer pulley today and also control the stepper motor. If that succeeds I plan on moving to the next phase and build the working frame. I plan on using the extruded aluminum like many 3D printers use for frames.
If you or anyone else is interested in my progress as I move through this project I can keep posting the little videos I make.
Thanks for your help so far.
David
The air and liquid are not coming on simultaneously. The air valve is open first then 100ms seconds later I open the solenoid for the liquid. After 500ms of them both being on I turn them both off simultaneously then pause for 2 seconds to start the cycle again. This is producing almost virtually no drippage from the valve but I have on occasion seen a build up and a rogue drip is produced. I will mess with the timing to see if I can totally eliminate that or a tiny drip once in a while is not going to be bad since the part will have moved past the nozzle by that time.
Last edited by DavyJones; - 30th September 2020 at 11:21.
I am interested in following your project. It's nice to see a real application being developed.
Thanks for posting
Sounds great I will keep posting to the thread as I go through my project... btw I am using a 12F683 since I had one laying around after my last project and I don't really need much for this. I'm setting up the stepper motor and about to give it a try in a few minutes.
David
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