Thanks Mark_S that makes sense to me know
David
Thanks Mark_S that makes sense to me know
David
David, at 200 steps per revelolution the motor will run rough. Once you get it running change the dip switches on the driver to 1/8th step or 1600 pulses/rev. It will run much smoother.
Mark
Last edited by mark_s; - 29th September 2020 at 00:05.
Mark thanks for the info. I'm new to working with stepper motors and their controllers. Seems a little easier to use a controller than to do all the programming to pulse all 4 inputs on the motor manually.
It looks like the NEMA rating just has to do with the size of the front or something here is the NEMA 23 one I got. It looks like this is rated 2.8 amps so would you mind I should set my controller dip switches to reflect 2.8 amps right?
Thanks
David
Normally I would design and build everything necessary to perform the tasks I need to with a PIC. In this case though to speed up development of my project I decided to use the stepper motor controller and relay module I am using to speed things up. The PIC is still doing all the work. I am working on a conveyer belt system that will move parts under a sprayer to get coated with a substance. I am controlling a solenoid to turn air on and off and a second solenoid to control dispensing the liquid, in this case for testing it is water. One thing I noticed since the nozzle is gravity fed and upside down as seen in my video, the gravity feed will produce a stream of water when the air is not engaged basically a constant drip so controlling the liquid flow (on and off) eliminates the drip. I did find no drip nozzles where I would only need to control the air flow but at $400 a pop that was not going to happen. The ones I am using are $20. My video is a mock up model for testing. I plan on adding a small conveyer pulley today and also control the stepper motor. If that succeeds I plan on moving to the next phase and build the working frame. I plan on using the extruded aluminum like many 3D printers use for frames.
If you or anyone else is interested in my progress as I move through this project I can keep posting the little videos I make.
Thanks for your help so far.
David
The air and liquid are not coming on simultaneously. The air valve is open first then 100ms seconds later I open the solenoid for the liquid. After 500ms of them both being on I turn them both off simultaneously then pause for 2 seconds to start the cycle again. This is producing almost virtually no drippage from the valve but I have on occasion seen a build up and a rogue drip is produced. I will mess with the timing to see if I can totally eliminate that or a tiny drip once in a while is not going to be bad since the part will have moved past the nozzle by that time.
Last edited by DavyJones; - 30th September 2020 at 11:21.
I am interested in following your project. It's nice to see a real application being developed.
Thanks for posting
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